Air Crash Daily | Continental Airlines Flight 1713 CVR Recording @AirCrashDaily | Uploaded July 2023 | Updated October 2024, 10 hours ago.
Social Media Links:
https://linktr.ee/aircrashdaily
Source(s):
youtu.be/xGkgwcIq9VM
dailymotion.com/video/x70pnkk
๐๐ผ๐ป๐๐ถ๐ป๐ฒ๐ป๐๐ฎ๐น ๐๐ถ๐ฟ๐น๐ถ๐ป๐ฒ๐ ๐๐น๐ถ๐ด๐ต๐ ๐ญ๐ณ๐ญ๐ฏ was a scheduled domestic passenger flight from Denver to Boise, operated by a Douglas DC-9 (Reg. N626TX) on ๐ก๐ผ๐๐ฒ๐บ๐ฏ๐ฒ๐ฟ ๐ญ๐ฑ, ๐ญ๐ต๐ด๐ณ.
Weather conditions in Denver were moderate snow and freezing temperatures. Following a 27 minute delay between deicing and departure, on takeoff the plane was over-rotated by the first officer. Control was lost, the plane stalled and impacted off the right side of the runway. Company procedures called for repeat deicing when in icing conditions if a delay exceeds 20 minutes. Confusion between the tower and the flight crew due to procedural errors resulted in the delayed takeoff clearance. Both pilots were inexperienced in their respective crew positions.
The captain had 33 hours experience as a DC-9 captain. The first officer had 36 hours jet experience, all in the DC-9. First officer demonstrated weak scan in training and had pilot performance problems with previous employers. First officer was on reserve, and had not flown for 24 days. The trip was assigned to the first officer for proficiency. Flight was first officer's 2nd trip as DC-9 first officer. Wing vortices from a landing plane on a parallel runway were not a factor in the accident.
๐ฃ๐ฟ๐ผ๐ฏ๐ฎ๐ฏ๐น๐ฒ ๐๐ฎ๐๐๐ฒ:
"The captain's failure to have the airplane de-iced a second time after delay before take-off that led to upper wing surface contamination and a loss of control during rapid take-off rotation by the first officer.
Contributing was the absence of regulatory or management controls governing operations by newly qualified flight crew members and the confusion that existed between the flight crew and air traffic controllers that led to the delay in departure."
Social Media Links:
https://linktr.ee/aircrashdaily
Source(s):
youtu.be/xGkgwcIq9VM
dailymotion.com/video/x70pnkk
๐๐ผ๐ป๐๐ถ๐ป๐ฒ๐ป๐๐ฎ๐น ๐๐ถ๐ฟ๐น๐ถ๐ป๐ฒ๐ ๐๐น๐ถ๐ด๐ต๐ ๐ญ๐ณ๐ญ๐ฏ was a scheduled domestic passenger flight from Denver to Boise, operated by a Douglas DC-9 (Reg. N626TX) on ๐ก๐ผ๐๐ฒ๐บ๐ฏ๐ฒ๐ฟ ๐ญ๐ฑ, ๐ญ๐ต๐ด๐ณ.
Weather conditions in Denver were moderate snow and freezing temperatures. Following a 27 minute delay between deicing and departure, on takeoff the plane was over-rotated by the first officer. Control was lost, the plane stalled and impacted off the right side of the runway. Company procedures called for repeat deicing when in icing conditions if a delay exceeds 20 minutes. Confusion between the tower and the flight crew due to procedural errors resulted in the delayed takeoff clearance. Both pilots were inexperienced in their respective crew positions.
The captain had 33 hours experience as a DC-9 captain. The first officer had 36 hours jet experience, all in the DC-9. First officer demonstrated weak scan in training and had pilot performance problems with previous employers. First officer was on reserve, and had not flown for 24 days. The trip was assigned to the first officer for proficiency. Flight was first officer's 2nd trip as DC-9 first officer. Wing vortices from a landing plane on a parallel runway were not a factor in the accident.
๐ฃ๐ฟ๐ผ๐ฏ๐ฎ๐ฏ๐น๐ฒ ๐๐ฎ๐๐๐ฒ:
"The captain's failure to have the airplane de-iced a second time after delay before take-off that led to upper wing surface contamination and a loss of control during rapid take-off rotation by the first officer.
Contributing was the absence of regulatory or management controls governing operations by newly qualified flight crew members and the confusion that existed between the flight crew and air traffic controllers that led to the delay in departure."